K20 Power now bolted in!

It took a while but I snuck a half day into working on the car with my dad. While I thought it was 3 hours of work it actually took 6.

First thing was to pull the k20a3 and remove the transmission and adapter plate.

Up next was moving those parts to the K20z3 and bolting them all back together.

From there we worked out what needed to be changed and we we removed and replaced a tube in the chassis. We also removed the old motor mounting plate and cut a new piece. After 5-10 minutes of welding we started to position the engine.

After measuring and cutting several tubes we had the left side mounted. Next we leveled the engine to 0.6 degrees and started on the driver side. They came out quite well

The final step was to check hood clearance. I didn’t expect it to fit but was nicely surprised. 3 mm to spare!

There week be some challenges with the steering and alternator but those are for a different day!

Ground clearance is a nice and acceptable 4″

Up next is the transmission mounts!

This engine is fighting me every step of the way!

From the moment I bought the engine it has fought me every step of the way. It seems the “Honda mechanic” that I bought it from was either a fantastic liar or had a love affair with red locktite.

I first realized it when I broke a 3/8″ extension trying to remove a flywheel bolt. I then brought out the impact wrench and it did absolutely nothing. A trip to the Chinese took store and coming home with an impact wrench that can make 800ft lbs of torque. The results? Nothing! Didn’t move it at all! Even tried heating the bolt to break the locktite but nothing changed.

Thankfully I have an amazing coworker that has the 1200lb version of the torque wrench. First thing it did was split the 12 point socket into 2. A trip to the orange store and $4 later I had a new 12 point 17mm socket. Given the first one slightly damaged the bolt head I decided to face off the new socket so it would have more grip and less of the rounded approach that makes sockets easier to get on to the bolt.

Unfortunately the bolt head on 2 of them bolts was too damaged. What happens next? Out came the welder! It took 3 attempts with the mig welder but adding a 3/4″ bolt did the trick finally. Most likely the heat of welding broke down any remaining locktite.

Up next I will put the engine back on the engine stand and verify the bottom end is good. And then we can start adding parts. The collection of “go fast parts” is growing!